EVALUATION OF COMMERCIALLY AVAILABLE IGNITRONS AS HIGH-CURRENT, HIGH-COULOMB TRANSFER SWITCHES*

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EVALUATION OF COMMERCIALLY AVAILABLE IGNITRONS AS HIGH-CURRENT, HIGH-COULOMB TRANSFER SWITCHES* R. Kihara University of California Lawrence Livermore National Laboratory P. O. Box 808, Livermore, CA 94550 Introduction New or improved switches are needed to meet the power requirements of multimegajoule glass laser Inertial Confinement Fusion (ICF) systems and Strategic Defense Initiative (SDI) weapons (e.g., mass drivers, railguns, and high-powered pulse lasers).i,2 These devices must switch high peak currents (>I x 106 A) and voltages (>20 kv), with an initial rate of current rise (di/dt) greater than 15 ka/~s, while transferring large quantities of charge (>103 C/pulse). The generated pulse will typically have a pulse width of 0.5 to 1.0 ms, measured at the Full-Width Half-Maximum (FWHM) or the 50% amplitude points of the waveform. The simultaneous attainment of these parameters in a repratable switch, has to our knowledge not yet been attained. A switch testing facility to proof and/or develop the required switches was built at the Lawrence Livermore National Laboratory (LLNL). The primary goal of this facility is to demonstrate repetitive, and simultaneous switching of I-MA, and 1,000-C per pulse, from either commercial or LLNL-designed switches. The published or advertised ratings for several types of high-current switches, which were considered for testing, are listed in Table I, these are: the size "D" and "E" ignitrons, the metal-to-metal contact switch, the moving-arc switch, and a heavy-duty spark gap of conventional design. All of these switches can be operated repetitively, except for the metal-to-metal contact switch, which is destroyed during the switching process. Of the remaining three switches the size "E" ignitron was chosen for the initial investigation because of its applicability to the laboratory's ICF program, and our belief based upon performance data for the smaller size "D" tubes3,4 that it had the greatest potential for development. The cross-section of an ignitron is shown in Fig. I, and a photograph of two size "E" tubes are shown in Fig. 2. The size "E" tube packages tested are approximately 23 cm in diameter by 56 cm long, and weighed 23 to 32 kg, depending on the tube model. The tube body is typically stainless-steel and is equipped with an integral water jacket for cooling. The cathode of the tube is formed by the body in combination with the mercury pool under the anode. In normal operation, conduction occurs preferentially between the anode, which is composed of graphite or molybdenum, and the mercury pool. Almost no current should flow to the stainless-steel walls. When the ignitron is in the off-state, the space between the two electrodes is insulated by a vacuum, allowing the ANODE CONNECTION Table I. Published or advertised ratings of various types of high-current switches, a Swi t ch Ignitron GL-8205 b NL-5553 c Peak Conduc- Voltage current Coulomb/ tion (kv) (ka) pulse time (ms) 25 600 325 <10 I 0 95 I, 150-30 ANODE Metal-tometal contact switch d 25 I,000+ 55 <0.2 Spark gap e 80 255 57 MERCURY II ~ l m l I B B I I ~ I ~ B B ~ ~ I BAFFLE Moving arc f 80 150 12 0.040 a b c d e f All switches can be operated repetitively except the metal-to-metal contact switch. Manufacturer's specifications for GL-8205. LANL. Aldermaston AWRE. Physics International. MLI SREMP. CATHODE j CONNECTION Figure I. Cross-section of an ignitron. IGNITOR * Work performed under the auspices of the U.S. Department of Energy by the Lawrence Livermore National Laboratory under contract number W-7405-ENG-48. 581

Report Documentation Page Form Approved OMB No. 0704-0188 Public reporting burden for the collection of information is estimated to average 1 hour per response, including the time for reviewing instructions, searching existing data sources, gathering and maintaining the data needed, and completing and reviewing the collection of information. Send comments regarding this burden estimate or any other aspect of this collection of information, including suggestions for reducing this burden, to Washington Headquarters Services, Directorate for Information Operations and Reports, 1215 Jefferson Davis Highway, Suite 1204, Arlington VA 22202-4302. Respondents should be aware that notwithstanding any other provision of law, no person shall be subject to a penalty for failing to comply with a collection of information if it does not display a currently valid OMB control number. 1. REPORT DATE JUN 1987 2. REPORT TYPE N/A 3. DATES COVERED - 4. TITLE AND SUBTITLE Evaluation Of Commercially Available Ignitrons As High-Current, High-Coulomb Transfer Switches 5a. CONTRACT NUMBER 5b. GRANT NUMBER 5c. PROGRAM ELEMENT NUMBER 6. AUTHOR(S) 5d. PROJECT NUMBER 5e. TASK NUMBER 5f. WORK UNIT NUMBER 7. PERFORMING ORGANIZATION NAME(S) AND ADDRESS(ES) University of California Lawrence Livermore National Laboratory P. 0. Box 808, Livermore, CA 94550 8. PERFORMING ORGANIZATION REPORT NUMBER 9. SPONSORING/MONITORING AGENCY NAME(S) AND ADDRESS(ES) 10. SPONSOR/MONITOR S ACRONYM(S) 12. DISTRIBUTION/AVAILABILITY STATEMENT Approved for public release, distribution unlimited 11. SPONSOR/MONITOR S REPORT NUMBER(S) 13. SUPPLEMENTARY NOTES See also ADM002371. 2013 IEEE Pulsed Power Conference, Digest of Technical Papers 1976-2013, and Abstracts of the 2013 IEEE International Conference on Plasma Science. Held in San Francisco, CA on 16-21 June 2013. U.S. Government or Federal Purpose Rights License 14. ABSTRACT 15. SUBJECT TERMS 16. SECURITY CLASSIFICATION OF: 17. LIMITATION OF ABSTRACT SAR a. REPORT b. ABSTRACT c. THIS PAGE 18. NUMBER OF PAGES 4 19a. NAME OF RESPONSIBLE PERSON Standard Form 298 (Rev. 8-98) Prescribed by ANSI Std Z39-18

Figure 3. Typical ignitron waveforms showing current (top) and voltage drop across the tube. Shot #400 on an NL-496: top (current) 50 ka/div, bottom (voltage) 500 V/div. Sweep rate is 100 ~s/div. Test Procedures Figure 2. Photograph of (left) an NL-496 and (right) a GL-8205, size "E" ignitrons. tube to hold off the applied voltage. The tube is switched on by applying a triggering pulse to the ignitor electrode, which is immersed in the mercury pool. A discharge forms between the mercury pool and the ignitor, filling the gap between the electrodes with ionized mercury vapor. Once the gap is filled, the mercury vapor supplies the medium for conduction, thereby switching the tube on. Test Circuit Description The test circuit was built around a large capacitor bank (56 mf @ 5 kv), rated at 700 kj, 280 C, and I-MA peak current, that had formerly been used for railgun studies. The circuit has two different configurations for testing switches. In the first configuration, the test circuit is operated as a critically damped RLC circuit. The charge transfer is limited by the storage capacity of the bank, or 280 Coulombs. A typical discharge waveform is shown in Fig. 3. All ignitrons to date were tested in this configuration. In the second configuration, parallel discharge circuits charge an inductor, which is crowbarred by the switch under test at peak current. This traps a slowly decaying, circulating current in both the inductor and the tube. The charge transfer is controlled by varying the L/R time constant of the inductor. For typical circuit values this can be greater than I,000 Coulombs. Test Limitations The test results and conclusions presented here should be considered tentative, as only two to three samples of each tube type were available for testing. Each sample within types was subjected to a different test, although corresponding pairs between types were tested identically, as described below. Characterization was complicated by the fact that samples in each type often varied markedly in their behavior under identical test conditions. All tubes were radiographed before testing to examine the internal geometry, and to check for mechanical problems which might predispose the tube to failure. After radiography each tube was mounted in the test stand and fired down at 25-100 ka to check for proper operation. Because of the limited number of samples the following test strategy was adopted. The "maximum current" level, which was defined as the current level required to cause failure in I-5 shots, was the first parameter to be determined for each tube. Starting at 150 ka for all tube types, the current level was stepped-up in increments of 50-75 ka, 5-shots were to be taken at each level until either tube failure occurred, or until the test limit (I-MA and 1,000 C/shot) was reached. Once the test limit was reached, lifetesting would have started at this level. If tube failure occurred before the desired current and charge level was reached, a second tube was installed and lifetested at 60% of the "maximum current" level. A tube failure was defined as either a failure to fire when triggered or a failure to hold voltage. A failure to fire caused by a shorted ignitor(s) was not counted as a failure if the ignitors could be cleared, by discharging a 12 uf, 6 kv pulser through it in the forward direction. The GL-37207a and the NL-496 were mounted in coaxial current returns, the GL-8205 was tested using the tube wall as a current return. Results None of the size "D" or "E" tubes tested survived the maximum current test. The General Electric GL-8205 failed at 525 ka, 168 C/shot (l-shot), and the National NL-496 failed at 475 ka, 151 C/shot (3- shots). The General Electric GL-37207a, a size "D" tube, reached 475 ka, 168 C/shot (6-shots). Failure of both "E" size tubes was caused by permanently shorted ignitors, both tubes still high-potted > 25 kv. The anode of the GL-37207a was deflected (-10 ) off of the tube axis by magnetic forces, after the 582

sixth shot. This was categorized as a failure, although the tube was still functional. Since all three of the tubes tested failed at similar levels, the current level for the lifetest was set to 300 ka. The GL-8205, which has a single ignitor, survived 500-shots at this level (112 C/shot). Ignitor shorts were cleared twice during the test after shots #52 and #129. The current on the same tube was then raised to 425 ka, where the ignitor failed permanently after two shots. The NL- 496 has two ignitors, and survived 435 shots (101 C/shot) before both ignitors failed. The first ignitor short occurred at shot #161, no attempt was made to clear it, and triggering was transferred to the second ignitor. After the failure of the second ignitor, neither ignitor could be cleared. Both size "E" tubes high-potted to > 25 kv after the completion of testing. The GL-37207a has two ignitors, and survived 250 shots (102 C/shot, before failure of the glass seal. The first ignitor short occurred at shot #155, triggering was then transferred to the second ignitor. The instantaneous arc drop was measured at the peak of the current waveform where the inductive component was zero. The variation of arc drop as a function of current was taken from the maximum current test, and is plotted in Figs. 4a,b,c. The statistical variation at one value of peak current was measured during the lifetest. For the GL-8205 @ 300 ka, this was 210-420 V for the first 50-shots, and 375-560 V, during the remainder of the test, varying widely from shot-to-shot. The mean voltage drop for 77 traces was 454 V, and the 2-sigma variation was 379-529 V. This corresponds to a tube resistance of 1.3-I.8 m~ over one standard deviation. The drop for the NL-496 @ 300 ka was 190-375 V over the duration of the test. The mean for 27 traces was 258 V, and the 2-sigma spread was 218-297 V, for a tube resistance of 0.7-I.0 m~ over one standard deviation. The drop for the GL-37207a (size "D") @ 300 ka was 190-260 V over the test. The mean voltage drop for 24 traces was 227 V, and the 2-sigma spread was 211-243 V. This corresponds to a tube resistance of 0.7-0.8 m~ over one standard deviation. This data has been summarized in Table 2. Conclusions Ignitor failure is presently the limiting factor in the high-current operation of the size "E" ignitrons. All of tubes tested showed a rapid drop in ignitor resistance with time. Without the use of a high energy pulser to clear the ignitors, the tube lifetimes given in this report would have been substantially shorter. The performance of the size "E" ignitrons was disappointing in comparison to the performance of the size "D," as the specifications of the "E" size, along with their greater physical size and mass, would tend to imply a similarly scaled capacity. Although the lifetested size "D" tube survived half as long as the size "E" tubes, the failure was mechanical in nature, and had the tube been physically stronger, we feel it would have matched the size "E" tubes in performance. Little effort has been made to re-examine the design of the ignitron, since it was invented in 1930's, except for a sporadic effort in the late fifties through mid-sixties.5, 6 It may be possible with new geometries, and a better understanding of the physics involved, to greatly expand it's capabilities. Acknowledgments The author would like to thank D. B. Cummings for his advice on the testing of ignitrons, and K. S. Leighton who provided the technical support required to make the test facility operational. Table 2. Summary of test results. Ignitron Charge Peak Maximum transfer/ Pulse Voltage current current shot width (kv) (ka) (ka) (C) (ms) No. of shots Tube drop (V) Tube condition di/dt (ka/~s) GL-8205 (size "E") Maximum rati ngs 25 600 Maximum current a 3 Lifetime b 2 375 10 -- 525 168 O. 32 c 300 -- 11 2 0.36 c NL-496 (size "E") Maximum ratings 25 100 -- 400 <150 Maximum current a 3 -- 475 168 O. 36 c Lifetime b I.85 300 -- 104 0.40 c GL-37207a (size "D") Maximum ratings 25 300 -- 50 O. 7 Maximum current a 2.7 -- 475 168 O. 36 c Lifetime b I.8 300 -- 102 0.36 c I 514 500 454 d 2 470 435 258 d 6 3OO 250 227 d failed 7.5 failing 3.5 -- 2.0 failed 6.25 failed 3.5 failed 6.25 failed 7.5 athe maximum current test determines the current level that causes tube failure in less than 5 shots. bthe lifetime test determines the tube lifetime at 60% of the maximum current level. Cpulse width was measured at half maximum. daverage tube drop at 300 ka. 583

600 500 500 - ~ "~ 400 400 - +- 300 300 " 200 aoo / + io0 ARC DROP GL-37207a io0 " FIG, 4c- ARC DROP GL-8205 I I i I I I = t00 200 300 400 500 600 Z (ka) lo0 200 300 400 500 600 Z (ka) 600 500 [I] References V. Bailey, P. Champney, J. Fockler, I. Smith,"Review of Switch Candidates and Preliminary Design of a Switch Test Facility for the Zeus Capacitor Bank," Report no. PSI-FR-154-02, January 1985, Pulse Sciences Inc., 14796 Wicks Blvd, San Leandro, Calif. 94577. 400 300 200 too /~ FIG, 4b- ~r ARC DROP NL-496 [2] R. S. Hawke and J. K. Scudder, "Magnetic Propulsion Railguns: Their Design and Capabilities," Lawrence Livermore National Laboratory, UCRL-82677, May 8, 1979. [3] K. Witham, D. Larson, B. Merritt, D. Christie, "Nova Pulse Power Design and Operational Experience," Lawrence Livermore National Laboratory, UCRL-95051, January 1987. [4] Private Communication, J. Melton, Summary of CTR experience with ignitrons at Los Alamos National Laboratory. 0 io0 200 300 400 500 500 I (ka] Figures 4a,b,c. Arc drop plotted against instantaneous current for the GL-37207a, NL-496, and GL-8205. The shaded bars represent the 2-sigma variation in drop recorded during the lifetest of each tube. [5] D. B. Cummings, "A Stabilized Switching Ignitron," Lawrence Livermore National Laboratory, UCRL-7391, published as "A Stabilized Ignitron," IEEE Transactions on Nuclear Science, NS-11, No. I, January 1964. E6] G. P. Boicourt and E. L. Kemp, "Development of Reliable 20 kv Ignitrons for Thermonuclear Research," Los Alamos Scientific Laboratory Report-LAMS-2416, December 1959. 584